Since I was not 100% certain of the proper method of blade balancing, I’ve started up this page. You see, until 9:00AM this morning I was certain how to properly balance blades. However, after reading the ALIGN Trex450SE instructions, which contain this diagram, I’m not at all certain.
Up until now, I had placed the blades trailing edges flat on a table, then tightened the balancing tool, and placed it on the jig. The objective was to have the trailing edges of the blades perfectly level. Here is what it looks like:
I hope you can see the difference in how I placed the blades together, compared to to what the Align manual suggests. Here is a closeup to help illustrate how I used to do this:
Compare this to using the ALIGN documented method:
As you can see here, not only does it appear quite different, so is the result! Using this method, my blades are out of balance. Or, are they?
Now, I’ve gone out and searched and consulted with the great oracles on this subject (the R/C discussion groups) and found the following:
On one of the most helpful sites I’ve found on the web, Mikey demonstrates the blade balancing using the same method, that seemed intuitive to me. Here is a screen shot from the video:
Checking another forum, I found the following this post that discusses first locating the COG (Center of Gravity) on the blades and marking them. Or balancing the COG on the blades so they are the same blade-to-blade, THEN getting them in dynamic balance:
http://www.rcgroups.com/forums/showthread.php?t=878885&highlight=blade+balancing
Hm. there seems to be MUCH more to getting a really great balance on your blades than meets the eye! With the vibration issues I’ve been happening, I’m going to do everything I can to provide as stable a main blade balance as possible.
What is most clear at the point, is that I have A LOT more reading to do. PART 2 will follow once I decide on exactly how I will be balancing my blades. The question of the afix orientation of the blades perists, even after I find the COG of the blades.
This link here looks to be the most concise explaination of a balancing method. [LINK]
I’ve had a few good flights, and few bad flights with the N450V2A. After locating a nasty wobble and some incorrectly manufactured parts, I’ve torn the bird down to just about the bare bones and have started a re-construction.
Starting here with this picture, I have already performed the following.
Replaced the Main bearings in the main bearing blocks. One of the old bearings had a bit of a ‘notchiness’ to it so I tracked down some replacement parts, including two pairs of original Align factory main bearings (5x11x5mm). $6.49.
They are installed at the top of the frame, and in middle, just above the main gearset (in blue). The main gearset has already been replaced with at genuine factory Align part AGNH1218$22.99
The original Pentium 30A ESC (Electronic Speed Control) was showing signs of overloading and causing in-flight resets! In defense of HobbyWing, it looks like I was running too steep a pinion on the main motor (I’ll get to that later). Regardless, I wanted to make SURE I did not have to learn auto-rotation landing in my first few weeks of flying. So I purchased a new genuine Align 35A ESC with Governor, PN 35ABLESC GOVMD5VBEC RCE-BL$53.99. It’s installed high on the frame now, where the battery would normally be located. I did this to help ensure good air flow along it’s heat sink.
As mentioned, it turns out the that original 13T pinon which came with the EXceedRC Alpha 400 63N18 motor is not an appropriate selection. It was suggest that I run either an 11T or 12T pinion by several people online. The local hobby shop had a pretty knowledgeable flyer behind the counter, and suggest a 12T would make a big difference. It’s also the suggested pinion for the factory Align Trec450 V2 (of which mine is a clone). Having already ordered an 11T pinion, I purchased the 12T. Original 13T is on the right, new 12T Align part on the left:
The motor itself might be OK. I’m going to re-use it for now. Another is on the way from Hobbypartz.com price about $20.00. The pinion is only firmly mounted on the shaft, since it will have to be precisely adjusted for main gear engagement once I re-install the motor in the frame.
Next I went about trying to get the main bearings and main shaft running as true and consistent as possible. The bottom bearing has some manufactured in lateral play, nothing I can do about that. But I did manage to snug up the shaft to bearing interface with some very light knurling of the main shaft where it contacts the lower bearing. Additional play looks like it will come out with a slight ‘cocking’ of the upper bearing. Just enough to produce a natural tendancy to run straight. I have plenty of bearings now. One of my next objectives will be to take the extra bearings I have to an expert bearing distributor and see if a higher-quality bearing is available in the same dimensions.
After all that work, the main shaft finally looks like it’s running true. The dial indicator is still picking up some movement, but it’s about 1/2 or perhaps less than it was originally. I think I managed to take at least a little play out of the main drive system, and that makes very hopeful for some major flight improvements.
Taking all these parts off, I think it wise to re-check the swash plate level, just in case it something got bent, twisted or otherwise tweaked. Placed the 450 swash leveling took on the plate, and it was dead on! I ordered the tool from XHeli.com (it’s an EXI too) for around $3.50. Well worth the investment. When I checked my ‘by eye’ leveling with the tool I found I was pretty far out. Sure it’s a fair bit more labor to tear down the head to use the tool, but having such a core component as close to perfect spec as humanly possible seems like a wise use of one’s time. Maybe it’s not, but I did it.
Having conquered my fears of the main shaft, time to rebuild the rotor head from the swash pate up. First thing I want to tackle is the top of the head, sort of going in reverse order. It turns out my latest blade grip purchase, to replace the broken grip, wss of the WRONG PART. My model is a Version 2, and the parts I got, unbeknown to me, were Version 1. Barely close, certainly not the cigar. Now today I did pick up a full compliment of Version 1 parts. Combined with the plastic Version 1 head ($7.99) and 2 pairs of grips($13.99) from the other day, I should be able to assemble a very tight and very functional main rotor head. My ideal scenario would be to re-use the original allow EXI head (left) instead of the new Align plastic Version 1 head (right).
It turns out the the V1 head (right) and the alloy V2 original head (left) are identical in width, and the ID of the feathering shaft ($7.99 for three) holes are also identical. The only difference (beyond material) is a more pronounced shoulder in the V1 head. Fit wise though, they tested out (to the best of my abilities) the same! This is very encouraging! All I need to do now is figure out how the V1 head systems is supposed to go together!
It’s about 1:00AM now. No need to work all night on this thing. I’ll pick this another day, maybe tomorrow, maybe I’ll go ride a motorcycle instead.
Wednesday was a pretty good day. It marked the arrival of a mini-DVR camera I’ve wanted to buy for quite some time. It went on sale for Fathers day at nearly 1/2 price. I just could not pass up the deal!
The location of the aperture is not perfect, but I can work with it. In fact I have a new canopy on the way from Hong Kong, that will be cut so I can mount the camera forward of main rotor head, and a little lower to make sure it’s not at risk of a blade strike. In the mean time I have a mount position rear of the main rotor that works OK. I like to have a little bit of the helicopter in view to give some perspective.
Here is an in-door run-up test of the camera.
Having found a suitable location, and even though I’ve still not sorted out the mystery vibration in the main drive train, I wanted to take it out for a flight, and shoot some POV video off the helicopter.
Here is the POV video:
Unfortunately, this was the aftermath of the crash. Broken main blade grip. That really annoying part is that this one of those 2% of the parts that is NOT directly ALIGHN TRex 450 compatible.
I’m able to source ALIGN 450 parts at the LHS (local hobby shop), but these design of these are so different that I don’t think I can use them. The bearings are the same size but they mount in different locations, and I think it’s allowing the blade grips to shift a few thousandths of an inch off-center, making what I know to already to be a nasty run-out on the main shaft, even worse. I’m fairly certain that it’s not an issue with the shaft itself, since I have 4 of them now (1 original and 3 replacements) and they are all showing the same runout when mounted in the drive system (video below shows the problem I am having).
You may notice wobble in the in-flight POV video. That’s not the camera. That’s actually the helicopter when it gets into this harmonic resonance with the main shaft vibration. It can be pretty nasty, and it certaily didn’t help me when I lost control and crashed.
I’m doing some research, consulting with the great oracles, and just trying to sort out the possible cause of the strange shaft run-out. So far, I’ve come across the solution, or solved this problem myself. Here is a video of the some testing I’ve done to quantify the issue:
After fighting with the gyro for a day, I finally cleared the programming on the DX6i and re-did ALL of it. I learned a few more things along the way. This is the final, current configuration that actually let me fly! I won’t pretend to say this is an optimal or even suggested setup, but it’s the one I came up with. Maybe this helps some others get their stuff off the ground.
DX6i EXI-450 Programming Ver. 2
Dual Rate & Expo
Aileron
Elevator
Rudder
AIL D/R 0
100%
INHibited
100%
INHibited
100%
INHibited
AIL D/R 1
100%
INHibited
100%
INHibited
100%
INHibited
Travel Adjust
Note: You need to move the sticks to access both travel directions, this was an important lesson!
Throttle
Elevator
Gyroscope
Aileron
Rudder
Pitch
↑100% ↓100%
↑125% ↓125%
↑100% ↓100%
←125% →125%
←100% →100%
↑125% ↓125%
Sub Trims
Throttle
Elevator
Gyroscope
Aileron
Rudder
Pitch
0
↑30
0
←17
→42
↑63
Gyro
0 (flap-0)
1 (gyro-1>
SW-GYRO
60.0%
70.0%
Throttle Curve
Low
1/4
1/2
3/4
Full
Normal
0 %
25%
50%
85%
100%
Stunt*
0 %
20%
40%
40%
40%
Hold
0.0 %
Pitch Curve
Low
1/4
1/2
3/4
Full
Normal
25%
50%
67%
82%
100%
Stunt*
15 %
25%
25%
25%
25%
Hold
0%
10%
10%
10%
10%
Swash Mixing
Swash
Aileron
Elevator
Pitch
– 60%
– 60%
+ 60%
Channel Mixing
Master
Slave
Rate D
U
Sitch
Trim
Mix 1
INHibited
Mix 2
INHibited
Revo Mix
UP
DOWN
Normal
0 %
0 %
Stunt
0 %
0 %
DX6i EXI-450 Setup Ver. 2
Reverse
Throttle
Elevator
Gyroscope
Aileron
Rudder
Pitch
Normal
Reverse
Normal
Reverse
Reverse
Normal
Swash Type
CCPM 120°
Throttle Cut
Position
ACTIVE
Dual Rate Combination Assignment
Dual Rate Switch
INHibited
Power Setting
B-US 247
* NOTE: I have set the Stunt settings for my own safety, not for actual stunt flying. If you use those settings you’ll end up with a bird in the ground, but at least it’s less likely to go full-throttle without you expecting if, if you do something really stupid (like me) and flip the mode from NORMAL to STUNT without thinking.
Following the re-build of the tail setup, removed gyro.. server testing.. reprogramming.. it all led up to the first *real* flight of the 450. Even in some pretty good wind!
Despite the bluster, the heli flew, and the gyro seemed to hold to any heading I set! This was FUN!
Despite bouncing off the pavement, I had a big fat grin as I walked home. I’d built the helicopter, I’d flown it, crashed it and flew it again. Now it’s time to learn to *really* fly this thing! 🙂
FRUSTRATION!!! Tried to fly but all I managed to do was cause the thing to spin like some sort of evil weapon. Despite my best efforts to solve the gyro issue, it was just not stable! At least the P-51 was treating me well yesterday. Even few it behind a long row of trees (accidentally) and it was still upright in the same slight banking turn it was when it suddenly went out of view. Even managed to land it on it’s wheels. Finally some R/C success.
So, going to the oracles on helicopter setup, it looks like the death spin was due to either sub-functional gyro (great..) or some other reason unknown. The gyro is brand new, and it initializes, reads inputs, applies compensation on yaw.. but.. just not working ‘right’.
Here is video my daughter shot while I was trying to sort the thing out.
When I thought I had it all figured out, I learned (in a rather painful way) that I in fact did not. At least no blood was spilled.
So, after a lot of testing with the heli double duct taped to the floor, I have some new settings that visually agree with my very limited understanding of how these things really work. One mental hurdle was figuring how how the Swash mixing really worked. A simplistic view of individual servos on the swash was getting me into a major logic box. It was when I looked at it from a conceptual standpoint, instead of the discrete mechanics, that it made sense. Confused? Join the club!
DX6i EXI-450 Programming Ver. 2
Dual Rate & Expo
Aileron
Elevator
Rudder
100%
INHibited
100%
INHibited
100%
INHibited
Travel Adjust
Throttle
Elevator
Gyroscope
Aileron
Rudder
Pitch
↓100%
↑125%
↑100%
←125%
→100%
↓125%
Sub Trims
Throttle
Elevator
Gyroscope
Aileron
Rudder
Pitch
0
↓10
0
→38
0
↓16
Gyro
INHibited
Throttle Curve
Low
1/4
1/2
3/4
Full
Normal
0 %
25%
50%
85%
95%
Stunt*
0 %
20%
40%
40%
40%
Pitch Curve
Low
1/4
1/2
3/4
Full
Normal
50 %
50%
67%
82%
100%
Stunt*
15 %
27%
62%
80%
100%
Swash Mixing
Swash
Aileron
Elevator
Pitch
– 60%
– 60%
+ 60%
Channel Mixing
Master
Slave
Rate D
U
Sitch
Trim
Mix 1
Throttle
Throttle
0%
0%
ON
INHibited
Aileron
Aileron
0%
0%
ON
INHibited
Elevator
Elevator
0%
0%
ON
INHibited
Rudder
Rudder
0%
0%
ON
INHibited
Gyro
Gyro
0%
0%
ON
INHibited
Pitch
Pitch
0%
0%
ON
INHibited
Mix 2
Throttle
Throttle
0%
0%
ON
INHibited
Aileron
Aileron
0%
0%
ON
INHibited
Elevator
Elevator
0%
0%
ON
INHibited
Rudder
Rudder
0%
0%
ON
INHibited
Gyro
Gyro
0%
0%
ON
INHibited
Pitch
Pitch
0%
0%
ON
INHibited
Revo Mix
UP
DOWN
Normal
0 %
0 %
Stunt
0 %
0 %
DX6i EXI-450 Setup Ver. 2
Reverse
Throttle
Elevator
Gyroscope
Aileron
Rudder
Pitch
Normal
Reverse
Normal
Reverse
Normal
Normal
Swash Type
CCPM 120°
Throttle Cut
POSITION – ACTIVE
Dual Rate Combination Assignment
Dual Rate Switch: – INHibited
Power Setting
B-US 247
* NOTE: I have set the Stunt settings for my own safety, not for actual stunt flying. If you use those settings you’ll end up with a bird in the ground, but at least it’s less likely to go full-throttle without you expecting if, if you do something really stupid (like me) and flip the mode from NORMAL to STUNT without thinking.
Not many photos were taken today since this was mostly transmitter programming, a little out of control flying and working on dialing in the Gyro. Still spent more than a couple of hours hacking away at understanding all there is to creating a BASIC setup for a good hobby helicopter. Now I have a better understanding of why RTF helis like the MadHawk typically don’t ship with an BNF (Bind-and-Fly) version. The amount of customer support they would have to deal with would quickly consume the fairly narrow profit margin.
Perhaps I’ll have the bird in the air this next week. For now I need to call it a night and get ready for another exciting week of computer programming, project management and cat wrangling.
The fourth day of construction starts with preliminary radio programming. Based on A LOT of information floating around on the web, I’m going to start off with the following settings for the bird. The manual for the radio itself is 139 pages, 80% or more of which are specific to the two primary programming modes, AEROCRAFT and HELICOPTER. I’ve said it before, I’ll say it again. The advances in R/C radios and equipment over the last 10 years is staggering.
NOTE: It turns out some of these preliminary settings were DEAD WRONG – Those in red were changed. See DAY 5 Setup for the corrected values!
DX6i EXI-450 Programming
Dual Rate & Expo
Aileron
Elevator
Rudder
100%
INHibited
100%
INHibited
100%
INHibited
Travel Adjust
Throttle
Elevator
Gyroscope
Aileron
Rudder
Pitch
↓100%
↑100% ↑125%
↓100% ↑100%
←100% ←125%
→100%
↓100% ↓125%
Sub Trims
Throttle
Elevator
Gyroscope
Aileron
Rudder
Pitch
0
↓32 ↓10
0
→40 →38
→23 0
0 ↓16
Gyro
INHibited
Throttle Curve
Low
1/4
1/2
3/4
Full
Normal
0 %
40% 25%
75% 50%
85%
95%
Stunt
100% 0%
90% 20%
80% 40%
90% 40%
100% 40%
Pitch Curve
Low
1/4
1/2
3/4
Full
Normal
50 %
50%
67%
82%
100%
Stunt
15 %
27%
62%
80%
100%
Swash Mixing
Swash
Aileron
Elevator
Pitch
+ 60% – 60%
+ 60% – 60%
+ 60%
Channel Mixing
Master
Slave
Rate D
U
Sitch
Trim
Mix 1
Throttle
Throttle
0%
0%
ON
INHibited
Aileron
Aileron
0%
0%
ON
INHibited
Elevator
Elevator
0%
0%
ON
INHibited
Rudder
Rudder
0%
0%
ON
INHibited
Gyro
Gyro
0%
0%
ON
INHibited
Pitch
Pitch
0%
0%
ON
INHibited
Mix 2
Throttle
Throttle
0%
0%
ON
INHibited
Aileron
Aileron
0%
0%
ON
INHibited
Elevator
Elevator
0%
0%
ON
INHibited
Rudder
Rudder
0%
0%
ON
INHibited
Gyro
Gyro
0%
0%
ON
INHibited
Pitch
Pitch
0%
0%
ON
INHibited
Revo Mix
UP
DOWN
Normal
0 %
0 %
Stunt
0 %
0 %
DX6i EXI-450 Setup
Throttle
Elevator
Gyroscope
Aileron
Rudder
Pitch
Normal
Normal Reverse
Normal
Normal Reverse
Normal
Reverse Normal
Swash Type
CCPM 120°
Throttle Cut
POSITION – ACTIVE
Dual Rate Combination Assignment
Dual Rate Switch: – INHibited
Power Setting
B-US 247
Once the Transmitting programming was complete, continuation of wire routing was undertaken. A quick trip to the electronics store for a bulk pack of tie wraps and large diameter heat shrink tubing got things back underway.
With the larger diameter shring tubing, I was able to put add it to both the motor and ESC wiring harnesses where they run along or through the frame. Better safe, adding a few grams of weight, than watching a helicopter catch fire because of a short.
7 wires from the Gyro are protected with the shrink tubing, where they will run through the frame. This is before using the heat gun to shrink.
My plan to apply shrink tubing in all areas where wiring is on or near the frame is working out well. The combined Gyroscope and elevator servo wire groups are protected where they will run between sections of the rear frame.
Preparing for first adjustments to blade tracking. Battery, canopy, ESC, motor all connected. Radio is not yet mounted because final tail servo setup has to be completed before finishing Gyro wiring and final radio installation.
Gyroscope and elevator servo wiring runs completed and secured. Radio will be mounted inside the frame just below re-entry point of the wiring harness. Shrink tubing covers wiring were it is near or in contact with frame.
More wiring work completed. Final securing of motor wires and ESC control harness (center to right), and primary AR6200 Receiver box with control wiring installed. Final radio installation has to wait for final servo setup, travel tuning and Gyro preliminary configuration.
30A Electronic Speed Control (ESC) secured to nose of frame. ESC is place are far forward as possible to help balance aircraft.
At this point, the blade tracking can be adjusted. Here is a video of the three runs in the shop to check and adjust blade tracking. One blade required 2 full turn reduction on connector length, the other blad required a single turn of extension to get blades tracking equally. VIDEO:
I only spent a couple of hours working on it tonight. I spent most of my time cooking for the kids. Tonight was no gourmet meal. However about 1/2 the time tonight was spent doing prep for tomorrow night. With 5 prime cuts of beef soaking up my proprietary beef rub overnight, it should be the basis of an enjoyable meal tomorrow.
So, with not much time I didn’t think I’d get much done. And, looking at the photos you’d probably ask how I spent 2 hours doing that. One word: soldering. One of the typically hidden, overlooked and far to often poorly done. Just for reference, here are some tips from Ask.com [LINK].
First, let me back track a little bit. As mentioned in yesterday’s post, I’d not been able to purchase a battery locally. Today, I took a chance and shot over to one of the really old-school hobby shops. It’s right next to the PLU campus in Parkland. As with all recent trips to the hobby shop, it wasn’t a cheap trip. I did, however, get a battery with a really nice mAh rating. The C level is fairly low (surge capacity) but for some training flights it might keep me out of trouble. And the price was pretty decent (about 1/2 of what other places were going to sell me much smaller battery for).
You can see in the photo here, the battery is a lot larger than the ‘big batteries’ for the MadHawk300. They look pretty wimpy in comparison (for reference, the MadHawk battery is the silver one marked ExceedRC on top).
It is only going to take about 3 1/2 hours to charge that battery with the wimpy little charger I have right now. That does not allow for much flying. :/
Back to the soldering story. The first step was to solder the Deans connectors onto the speed controller (aka ESC). Soldering the speed controller was a breeze. Good quality wire bound to the Deans connectors quickly. That was easy!
What I spent probably an hour fighting with are the cheap micro-hair stranded aluminum wire on the battery I picked up today. It’s one of those things you just can’t see when you purchase them, since they typically already have some sort of connector affixed. Sadly, not the connector type I want to use. Here is a close up of a Deans connector I’ll be using.
But I did get the soldering completed, after destroying one set of Deans connectors doing it. Quality of the joints are highly suspect, but they seem to be mechanically sound (tested). Voltage check on the battery before and after affixing the connectors did not indicate any measurable voltage drop due to resistance in a bad solder joint.
Here is a photo of the final production, on the ESC. I don’t plan to post a photo of the battery connector and soldering work. It’s an embarrassment. But after 3 attempts, one destroyed connector and starting to run out of wire for the battery, it’s going to have to be sufficient.
With a 3-cell battery, connectors attached to battery and speed controller (ESC), I was able to finally power up the AR6200 long-range receiver and get it bound to the DX6i radio.
One of the nice things about the DX6i, is it’s 10 model memory. Plus it has the ‘safe model’ feature. If you accidentatly forget to select the right model file for what you are flying, the RX and TX won’t talk to each other. RX binding data is retained with the model configuration. The concept here is to keep you from firing up your cool Delta Dart ducted fan jet, and taking off, only to find you’d left the transmitter configured for a conventional aircraft. That can create a REAL mess when you grab a stick full of elevator. The DX6i won’t like kind of mistake happen.
With power on the system, plugging in the servos allowed preliminary servo horn positioning and fine tuning with the sub-trims. Just in case I lose my programming on the bird, I’m going to document the subtrims and other settings on this page:
Sub-Trims EXI-450 V2 & Spektrum DX6i
Throttle
0
Aileron
+40
Elevator
+32
Rudder
+23
Gyro
0
Pitch
0
So, here is the current state at the end my tonight’s short work session. As you can see, there is a lot of work left to do. It still does not even look much like a helicopter yet.
Spent a couple more hours working on the 450 last night. It’s coming along nicely. Today I didn’t need to grind anything.
A couple of the many tasks required to get this thing in the air, is balancing the main blades and applying Loctite to all metal to metal fasteners. To accomplish this I needed some very small metric hardware and a new tube of low-power Loctite. A lot of people are using Blue Loctite 242.
I don’t think it’s the proper compound for fasteners of the size we’re using, so purchased a large bottle (all they carried at the store) of the Purple Loctite 222.
The place I like to go for such things is Tacoma Screw (there is one local in my town, about 35 miles from Tacoma itself – for this I’m glad). It’s a jobber style shop with top-notch customer service, curious people behind the counter (by that I mean they like to talk about what you are working on) and always friendly. I picked up a pair of German Philips #0 and #00 screwdrivers:
Also picked up 100 2mm washers:
And finally, a long 2.5mm bolt and nylocks for making a home-brew pour-boy blade balancing rig:
I ran one of the nylock nuts down on the screw, about 2/3 of the way. Placed the blades on the bolt and ran down the other nut, just making them snug. I chose the nylock nuts because I knew that they would stay put once I achieved the snugness wanted. A few extra pennies spent to save a lot of potential frustration later. You learn these sorts of things being a gearhead for nearly 4 decades.
The frame on the EXI-450 Plastic V2 is made of a stamped metal (you know, I think it’s aluminum, but I’ve not confirmed that), so some of the edges are rather sharp. To prevent the cutting/chaffing of wires where they exit the frame, I placed a small bit of high-strength tape (red) on the frame and then places a heavy duty heat shrink tubing over the wire bundle and applied heat to shrink with a heat gun, which works orders better than a lighter. You can get a cheap heat gun at Chinese places like Harbor Freight for around $10.
Here is the reciever I plan to use for this helicopter. It came with the Spektrum DX6i transmitter I purchased last month, and have been using with the ParkZone P-51 and Blade CX3. Not in this photo is the 2nd remote antenna/receiver that provides a very long range capability.
Installing the linkage balls on servo horns was next. The idea here is to make sure the link bars are as perfectly vertical as possible when installed on the servo, so some trail and error is required to select the correct hole to mount the balls. In this case both of the forward servos were able to use the last hole. You’ll notice that the balls are mounted in ‘reverse’ so the ball is on the servo’s side of the arm. Once they are all installed and photos taken, the reason for this will be clear.
Unfortunately, not all servo placements allow for such cut-and-dried installations. To get as close to pure vertical actuator alignment, you sometimes have to get a little fancy with the servo hardware. Once again, out comes the cheap Harbor Freight heat gun to apply some ‘persuasion’ to the nylon horn. After determining how much offset I needed, it was made very hot and then adjusted.
I think this makes it a little clearer why the adjustment was made and how it all turned out. This is the pitch cyclic primary servo.
The fly bar on a Bell-Hiller head is critical to smooth and stable flight. To get the fly bar properly setup, the first thing that has to be done is make sure it’s absolutely centered. Measuring with a caliper seems like a pretty accurate method.
Larger photo of the Bell-Hiller rotor head, typical to R/C helicopters.
Unlike yesterday, I placed the ‘calling it quits for the day’ photo at the end of this post.
It’s looking a lot more like a helicopter now! I still need to get some important things before I can go much further, the most critical of which is my batteries! I think I mentioned it in the last post, being unable to source a suitable battery at the local hobby shop, soooooooooooo yet another package of stuff is on the way. I’m sure I could have save $30-40 on shipping if I’d spec’d out my needs better ahead of time. For someone that is such a stickler for planning, I didn’t do a very good job of it for this project so far! :p